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打筛模式在造纸法再造烟叶生产中的应用实践
Application and Practice of Refining-Screening Mode in Reconstituted Tobacco Production by Papermaking
收稿日期:2022-04-22  
DOI:10.11980/j.issn.0254-508X.2022.09.018
关键词:  中浓压力筛  低打浆度  高湿重  高吸收性
Key Words:medium concentration pressure screen  low refining degree  high wet weight  high absorbability
基金项目:
作者单位邮编
李龙* 上海烟草集团太仓海烟烟草薄片有限公司江苏太仓215433 215433
林晓林 上海烟草集团太仓海烟烟草薄片有限公司江苏太仓215433 215433
张大坤 上海烟草集团太仓海烟烟草薄片有限公司江苏太仓215433 215433
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摘要:采用中浓压力筛与回流立管的组合形式,对传统再造烟叶浆料的处理模式进行了系统性优化,由单一的“打浆”模式升级为“打筛”模式。在保证浆料匀度的前提下,实现了“低打浆度,高湿重”的浆料处理预期,其中压力筛出口良浆打浆度从46°SR降至34°SR,降幅26.1%;湿重从3.1 g提升至4.1 g,升幅32.3%。由此浆料生产得到的基片透气度从2300~2500 mL/min提升至4000~4200 mL/min,提升幅度超过70.0%,匀度指数从342提升至371,提升幅度为9.1%,基片正面静摩擦力从93 N提升至112 N,提升幅度为20.4%,接触角变化速率从2.8°/s提升至4.6°/s,提升幅度为64.3%。按7500 t的年产量计算,打筛模式的制浆能耗成本可降低36.41万元/a。
Abstract:The processing mode of reconstituted tobacco pulp was optimized from traditional refining mode to refining-screening mode through the combining form of medium concentration pressure screen and backflow stand pipe. Based on the ensurance of pulp uniformity, the refining-screening mode realized low refining degree and high wet weight of pulp. The results showed that compared with traditional refining mode, the refining degree of finished pulp decreased from 46°SR to 34°SR, decreasing by 26.1%; wet weight increased from 3.1 g to 4.1 g, increasing by 32.3%; the air permeance of substrate increased from 2300~2500 mL/min to 4000~4200 mL/min, increasing by more than 70%; uniformity index increased from 342 to 371, increasing by 9.1%; static friction of the front of base sheet increased from 93 N to 112 N, increasing by 20.4%; instant absorbability increased from 2.8°/s to 4.6°/s, increasing by 64.3%. Moreover, based on the annual output of 7500 t, the pulping energy cost under refining-screening mode could decrease by 0.3641 million CNY every year.
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